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Inappropriate directional control inputs after touchdown lead to runway excursion

01 Aug 2022
On 21 November 2019, with variable cross/tailwind components prevailing, a Boeing 737-800 went around from its first ILS approach to Odesa before successfully touching down from its second. It then initially veered left off the runway before regaining it after around 550 metres with two of the three landing gear legs collapsed. An emergency evacuation followed once stopped. The Investigation attributed the excursion to inappropriate directional control inputs just before but especially after touchdown, particularly a large and rapid nosewheel steering input at 130 knots which made a skid inevitable. Impact damage was also caused to runway and taxiway lighting.

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Source Skybrary

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